| 40135 (D335, 97406)
This locomotive was from the batch of twenty
(D325 to D344) built with 'split-box' type headcode. Train
identification roller blinds were housed in illuminated units on
either side of the nose ends. This enabled interconnecting gangway
doors to be fitted. These were a little-used facility for crew
changing purposes on 'double-headed' locomotive workings. This
same locomotive batch included the notorious D326, involved in the
'Great Train Robbery' of 1963 and various other incidents.
40135 was built by English Electric at Vulcan
Foundry, Newton-le-Willows, entering service on 11th March 1961
allocated to 5A Crewe North. She was later reallocated in April
1966 to Western Lines, June 1968 to D05 Stoke Division, May 1969
to D09 Manchester Division, Jan. 1972 to D08 Liverpool Division,
May 1973 to Springs Branch, August 1973 to Carlisle Kingmoor, and
May 1975 to Longsight, where she remained until withdrawal on 22nd
Jan. 1985.
From this point, the locomotive led something
of a charmed life. Thanks to behind-the-scenes intervention, the
loco avoided a very close call with the cutter's torch at
Doncaster Works. Having survived scrapping, she was one of four
Class 40's miraculously returned to departmental traffic in May
1985, for use in the remodelling of Crewe Station approaches.
Based at Crewe Diesel TMD and renumbered to 97406, she and the
other three 97's worked around Crewe and on various other freight
duties in the London Midland Region.
Final withdrawal from British Rail service came
on 16th December 1986. Thankfully, further intervention prevented
the loco from reaching Swindon Works for scrapping. After
painstaking negotiations and discussions, 40135 was put onto the
BR tender list, along with 40012. The CFPS successfully tendered
for the loco in May 1988, and she was delivered to Bury later that
year.
The CFPS carried out their first locomotive
repaint on 40135 during the summer of 1991 to a very high
standard. Steam heating was restored in December 1991, which
included the re-manufacture, virtually from scratch, of the boiler
water tanks. The loco then went on to become a reliable ELR winter
passenger loco for a considerable period. The Clayton steam heat
generator was subsequently transferred to 40145. A light overhaul
of the power unit was completed in 1997.
The loco unfortunately suffered engine damage
in April 1998. After lengthy repairs, D335 was successfully
restarted in September 2000, in time for the ELR Diesel Gala.
Following this, bodywork restoration and a repaint into rail blue
were completed for the ELR July 2001 Diesel Event. Steam heating
was again restored to the locomotive in January 2002.
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